The Simulated weather for Sunday was Rain all day. The Reality was that after 10am it did not really rain again until 4:00pm. So I went flying. I'm currently working on altitude hold, but the wind was really gusty gusting from 5 to 20mph. A helicopter takes less energy to fly when moving than when it is hovering. If you try to hover in one spot with gusty winds the helicopter balloons up and down as the wind speed increases and decreases. This makes it very hard to sort out the altitude hold loop as you are never sure if the up and down is wind or oscillation's. I could hover lower and get a better handle on how the altitude loop gain is but until I have it hovering at high (recoverable) altitude I'm not going to play with the altitude hold down low. The altitude hold will have to wait until a calmer day.
So since I could not do altitude hold I thought I'd work on heading hold. In flying around with the magnetic heading hold engaged the helicopter seems relatively stable but the tail wandered a few degrees each way. I always thought that it was some local magnetic variation, that may contribute, but in looking at the data the tail target vs actual error is often 3 to 6 degrees and it wanders a bit. It seems to hold an offset. The standard way to fix this in a control loop is to add some integral error term and the result is The oscillation's you see on the left. So I turn down the I term (to 5% of the P term) and turn up the D term and its better, but still not ideal. You can still see some 3 to 4 second oscillations when steady and a fair bit of overshoot when perturbed. I'd been doing the default PID tuning of turning the P gain up to the point where it just starts to oscillate and taking the Ziegler-Nichols values you can find on the web. I conceptually understand what is going on, but this is straining my control system theory. (My only official control theory class was all done as laplace transforms in 1983) Early in my professional career(1985 to 1991) I did a fair number of analog and mixed analog/digital control systems, but always with a adult supervision from a controls person. Since 1991 I've mostly been a software coder. So in trying to relearn all of this I have a several specific questions that I'd love have any lurking control theory guys help me with.
Most control theory books, articles and tuning discussions assume you have a linear plant. In reality most of my "Plants" will be integral in nature. IE I do not control the thing I'm trying to close the loop on directly, I really control the acceleration or rate. So there are one or two physical integrals between my control input and the thing I want to control. See the example to the left.
If I just close the loop around the whole thing, its going to be really unstable. So my plan was to have Target Position yield Target Velocity Target Velocity yield target Pitch and Target Pitch yield Pitch Rate. This would have hard limits for each intermediate step. IE max velocity will be 5m/sec, regardless of the position error. Clearly every intermediate step in this will have a proportional gain term, any advice on which ones should have integral terms and when I should reset the integrals to zero?
I'm also struggling with a stupid simple question I have about PID terminology. You can express a PID as
control= P*(error+I*integral+D*difference_or_rate)
or You can express a PID loop as
control = (P*Error)+(I*Integral )+(D*difference_or_rate)
When you look at the standard Ziegler-Nichols chart :
for PID P = .6Gu I=2/PU D=PU/8 Is this for the first form or the second? When you measure Pu I assume Pu is the oscillation period in samples (this is a discrete system), or have I made a wrong assumption here?
Lastly is the guidance for standard linear PID tuning even valid for this sort of plant? If not can one provide some guidance on tuning such loops?
Reasonable people adapt themselves to the world. Unreasonable people attempt to adapt the world to themselves. All progress, therefore, depends on unreasonable people. - George Bernard Shaw.
Monday, January 28, 2008
Sunday, January 27, 2008
It Never Rains in Southern California
Notice the Probability of precipitation line...90% at 1AM 100% for the rest of the day. No FLying today.
Saturday, January 26, 2008
Pavlov's Pilot
After two outings where I hit the altitude hold switch and I crashed, I was hesitant to test again. I reluctantly went out to test fly the helicopter today and on the second flight I got up the courage to hit the altitude hold switch and things seemed to work. I failed to get data from the second flight for some reason, probably has to do with the software in the Telemetry box not logging restarts correctly, but I'm not exactly sure why I got no data. I'm ready to test again in the morning.
Last Crash
The last crash was a bit violent. You can see the crushed tin that held the formerly working GPS.
I did not take a picture of the crashed helicopter, but here are some of the broken pieces extracted from the trash.
I was planning to replace the GPS with the new smaller differential capable GPS so I
packaged that in an altoids tin, its about 1/3 the size of the old GPS.
Here it is rebuilt and ready to try again. To get a concept of the amount of work, the main frame on the helicopter is flat carbon fiber plate, in the broken pieces picture you can see that both side plates were broken.
I did not take a picture of the crashed helicopter, but here are some of the broken pieces extracted from the trash.
I was planning to replace the GPS with the new smaller differential capable GPS so I
packaged that in an altoids tin, its about 1/3 the size of the old GPS.
Here it is rebuilt and ready to try again. To get a concept of the amount of work, the main frame on the helicopter is flat carbon fiber plate, in the broken pieces picture you can see that both side plates were broken.
Friday, January 25, 2008
Another Altitude hold crash...
I crashed again this morning before work. I know that I had all the mode switches in the right place in the right order. This is very frustrating!!! ARGHHHHHHH
A brief look at the data implies that the Gain was just WAYYYY to high, but it should be identical to the flight gain where the helicopter did perfect altitude hold. This time in addition to th parts listed form the last crash I broke the tail boom and side frames. I see at least 8 hours of work to be flying again. I'm going to have to find a way to sneak up on this one as its getting expensive.
A brief look at the data implies that the Gain was just WAYYYY to high, but it should be identical to the flight gain where the helicopter did perfect altitude hold. This time in addition to th parts listed form the last crash I broke the tail boom and side frames. I see at least 8 hours of work to be flying again. I'm going to have to find a way to sneak up on this one as its getting expensive.
Thursday, January 24, 2008
New GPS boards...
The adapter board to wire up the new GPS arrived on Tuesday,
I finally got to assemble them today. I've got to make a shield can for the helicopter and an antenna mount for the Telemetry suitcase and I can start testing with the differential GPS. Tonight the GPS is hooked up to the antenna on my roof and I'll record 12 hours at 10Hz and see how much things move around. the picture below shows that my house has moved 4.36M in altitude and 1.29 and 2.77 in lat and lon since I started the GPS recording positions 4 hours ago.
Not too bad for an unaided GPS iin the rain partially under a tree.
I finally got to assemble them today. I've got to make a shield can for the helicopter and an antenna mount for the Telemetry suitcase and I can start testing with the differential GPS. Tonight the GPS is hooked up to the antenna on my roof and I'll record 12 hours at 10Hz and see how much things move around. the picture below shows that my house has moved 4.36M in altitude and 1.29 and 2.77 in lat and lon since I started the GPS recording positions 4 hours ago.
Not too bad for an unaided GPS iin the rain partially under a tree.
Some simple Trig
Last night after I finished reassembling the helicopter I did some software work on the helicopter simulator . The sim is a full 3D 6DOF helicopter simulator with display. I downloaded it about 9 months ago and it works well. It was part of the source forge helicopter autopilot project. I've been using it to develop control laws for the real helicopter. Last night I changed my simulator control laws from having yaw always north facing to putting in a full transform from North, East to Forward Right for the position and velocity feedback loops. My helicopter sim now flies the full NG-LLC flight profile while doing slow 2 deg/sec rotations the whole time. It all works so the next stop for this code is the "real world " helicopter.
Wednesday, January 23, 2008
Crash Gordon and the Helicopter(s).
My Son came down from the bay area to visit this weekend so I did not get much unreasonable work done.
Crash #1 On Sunday we were going to a play in balboa park and I had 30 minutes to kill. so I was flying the little fully manual trex 450 in the driveway. While I was doing this my wife came out and started moving the garbage cans toward the curb. I was in the way so I landed the trex next to the truck, shut down and preceded to take off the neck strap on the transmitter so I could help with the trash, in the process of doing this I hooked the throttle hold switch with the neck strap and the helicopter spattered itself all over the side of the truck. Its a good thing the trash cans were not yet at the curb, I had additional material!
Background for Crash #2.
On the last reported test flight altitude hold worked very well, but I had not yet tested clmb and descent. So I made two minor software changes, I added limits to the vertical velocity. (Vertical velocity had just been the differential term in the alt hold PID, but I spluit that in half so I could explictly limit vertical velocity. )I reprogrammed the mode switch to facilitate testing this. The Mode switch has three settings mode 0, 1,2 Mode 0 has always been manual.
Mode 1 was rudder heading hold, mode 2 was Altitude and Rudder hold. I changed this so both Mode 0 and Mode 1 were manual and Mode 2 was automatic Rudder and altitude.
I also recorded the target Altitude , Heading and initial collective value when going from mode 0 to mode 1. The idea being that I could set my target altitude by toggling from 0 to 1 then manually deviate from this position and go to it when switching to mode 2.
I went and test flew this combination on Tuesday Morning. In the process of adding the velocity limits I'd changed a feed back sign and altitude hold went the wrong way... I started above my target and when engaged the helicopter accelerated up at ever increasing rates. I tried this twice and figured out what was wrong and called it a day after 45 seconds of flying.
I changed the software sign last night and went out this morning to test the change.
Crash #2
I did my usual preflight routine I made sure that all the controls on the helicopter moved in the correct direction. (In past S/W version this was also a test to insure I was in mode 0, because in mode 1 rudder would not respond) So I brought the helicopter to a stable hover about 30 feet in front of me at about 15 to 20 feet of altitude. I then proceeded to flip the mode fro0m mode 0 to mode 1, alas it was already in mode 1 and I went to mode 2. Realize that while manually flying a helicopter you can't look down at the transmitter to check switch positions. It must have gotten bumped into mode 1 while I was hooking up the main propulsion battery or starting the video camera. So when it went from Mode 0 to Mode 1 it was at altitude 0 and full down collective. So when I went to mode 2 its target altitude was 0 and its initial guess for the collective position was full down. This is a fully acrobatic helicopter so full down collective is at least 3 negative gees. Before I could react the helicopter was on the ground, hard.
Broken parts: Both skids,flybar, flybar paddles, both blades, GPS antenna mount, one blade grip ball end, battery tray and the Jesus bolt. (the bolt that holds the main rotor to the airframe is called the Jesus bolt) total damage about $120.00 with the majority of that being the blades.
I had spares of most of the parts. Tonights task was to reassemble the helicopter. Its done, but not tested yet, I'm letting the glue on the GPS antenna mount dry while I type this.
(After glue dried tested all electronics and systems all check out ok, ready for blade tracking in the AM weather permitting.)
Crash #1 On Sunday we were going to a play in balboa park and I had 30 minutes to kill. so I was flying the little fully manual trex 450 in the driveway. While I was doing this my wife came out and started moving the garbage cans toward the curb. I was in the way so I landed the trex next to the truck, shut down and preceded to take off the neck strap on the transmitter so I could help with the trash, in the process of doing this I hooked the throttle hold switch with the neck strap and the helicopter spattered itself all over the side of the truck. Its a good thing the trash cans were not yet at the curb, I had additional material!
Background for Crash #2.
On the last reported test flight altitude hold worked very well, but I had not yet tested clmb and descent. So I made two minor software changes, I added limits to the vertical velocity. (Vertical velocity had just been the differential term in the alt hold PID, but I spluit that in half so I could explictly limit vertical velocity. )I reprogrammed the mode switch to facilitate testing this. The Mode switch has three settings mode 0, 1,2 Mode 0 has always been manual.
Mode 1 was rudder heading hold, mode 2 was Altitude and Rudder hold. I changed this so both Mode 0 and Mode 1 were manual and Mode 2 was automatic Rudder and altitude.
I also recorded the target Altitude , Heading and initial collective value when going from mode 0 to mode 1. The idea being that I could set my target altitude by toggling from 0 to 1 then manually deviate from this position and go to it when switching to mode 2.
I went and test flew this combination on Tuesday Morning. In the process of adding the velocity limits I'd changed a feed back sign and altitude hold went the wrong way... I started above my target and when engaged the helicopter accelerated up at ever increasing rates. I tried this twice and figured out what was wrong and called it a day after 45 seconds of flying.
I changed the software sign last night and went out this morning to test the change.
Crash #2
I did my usual preflight routine I made sure that all the controls on the helicopter moved in the correct direction. (In past S/W version this was also a test to insure I was in mode 0, because in mode 1 rudder would not respond) So I brought the helicopter to a stable hover about 30 feet in front of me at about 15 to 20 feet of altitude. I then proceeded to flip the mode fro0m mode 0 to mode 1, alas it was already in mode 1 and I went to mode 2. Realize that while manually flying a helicopter you can't look down at the transmitter to check switch positions. It must have gotten bumped into mode 1 while I was hooking up the main propulsion battery or starting the video camera. So when it went from Mode 0 to Mode 1 it was at altitude 0 and full down collective. So when I went to mode 2 its target altitude was 0 and its initial guess for the collective position was full down. This is a fully acrobatic helicopter so full down collective is at least 3 negative gees. Before I could react the helicopter was on the ground, hard.
Broken parts: Both skids,flybar, flybar paddles, both blades, GPS antenna mount, one blade grip ball end, battery tray and the Jesus bolt. (the bolt that holds the main rotor to the airframe is called the Jesus bolt) total damage about $120.00 with the majority of that being the blades.
I had spares of most of the parts. Tonights task was to reassemble the helicopter. Its done, but not tested yet, I'm letting the glue on the GPS antenna mount dry while I type this.
(After glue dried tested all electronics and systems all check out ok, ready for blade tracking in the AM weather permitting.)
Saturday, January 19, 2008
Two controls down, two (hard ones )to go
I flew the helicopter this morning.
First time with altitude hold. The Autopilot does a MUCH better job of altitude hold than I do. Next Up (Sunday?) Pitch and Roll. this was also the first flight with airborne video, I'm not going to post the video because the camera was oscillating up and down and watching it makes one sea sick.
(I also pointed it too far down so 8 minutes of the dirt in a dirt parking lot would not be worth much.) I'll try to improve the angle and the mount before the next flight. The Ultimate Camera Helicopter would be: (http://www.bergenrc.com/ObserverTurbine.php, or maybe http://www.bergenrc.com/Observer.php)
The next steps will be
1)Pitch and Roll to Elevator and Alieron PIDs, where the RC system provides commanded pitch and roll angles.
2)Vforward and Vright velocities provide Desired Pitch and Roll where the RC system
provides desired Vforward and Vright.
3)GPS position hold -> Gives desired Vnorth and Veast ->yielding desired Vforward and Vright.
First time with altitude hold. The Autopilot does a MUCH better job of altitude hold than I do. Next Up (Sunday?) Pitch and Roll. this was also the first flight with airborne video, I'm not going to post the video because the camera was oscillating up and down and watching it makes one sea sick.
(I also pointed it too far down so 8 minutes of the dirt in a dirt parking lot would not be worth much.) I'll try to improve the angle and the mount before the next flight. The Ultimate Camera Helicopter would be: (http://www.bergenrc.com/ObserverTurbine.php, or maybe http://www.bergenrc.com/Observer.php)
The next steps will be
1)Pitch and Roll to Elevator and Alieron PIDs, where the RC system provides commanded pitch and roll angles.
2)Vforward and Vright velocities provide Desired Pitch and Roll where the RC system
provides desired Vforward and Vright.
3)GPS position hold -> Gives desired Vnorth and Veast ->yielding desired Vforward and Vright.
Friday, January 18, 2008
Smart helicopters...
A good read on automating a helicopter.
http://sun-valley.stanford.edu/papers/Conway:95.pdf
http://sun-valley.stanford.edu/papers/Conway:95.pdf
Control Stratagey
The four things I can control are: Rudder, Collective, Elevator, Aileron.
My scheme for control is to use a set of PID loops.
Most likely some of these will only have P gain, but the concept is to use the following:(Copied from code) The PIDs marked with * in the comments will be different in the rocket.
OnePidElement Yaw_to_Rudder; //Takes IMU yaw and drives rudder *
OnePidElement Alt_to_VSpeed; // target altitude drives desired vspeed.
OnePidElement VSpeed_To_Collective;// desired vspeed drives collective.*
OnePidElement Pitch_To_Elevator;//desired pitch drives Elevator.*
OnePidElement Roll_To_Alieron;// desired roll drives Alieron.*
OnePidElement V_Forward_To_Pitch;//desired Vforward drives pitch.
OnePidElement V_Right_To_Roll; //desired Vright and drives roll
OnePidElement Long_to_V_East; //desired Longitude and drives VEast.
OnePidElement Lat_to_V_North; //desired Lattitude and drives VNorth;
And one more conversion function:
void ConvertDirection(double V_North, //Desired V_North input
double V_East,//Desired V_East input
double Yaw,//Current True YAW corrected for magnetic deviation input,
double &V_Forward,// Converted V_Forward target out
double & V_Right, //Converted V_Right target out
);
OnePidElement is an object that holds the a PIDGainConstants object and the current integration state.
The Yaw to rudder , Pitch to Elevator and Roll to Alieron PIDs will be run for each IMU sample.
All other PID's will be run for each GPS data set.
I'm not planning to integrate the accelerometers. (Yet)
An example would be:
Elevator=Pitch_To_Elevator.DoServoPidAdjust(target_pitch, imu.pitch , imu.x_rate);
Each OnePidElement contins a PID gainObject that has the following gain limit elements:
double p_gain;//Proportional Gain
double i_gain;//Integrator Gain;
double d_delta_gain; //Sample to Sample delta gain
double d_meas_gain; //Rate as measured by IMU or GPS
double max_i_windup;// Maximum integrator value limit.
double min_i_windup;//Minimum integrator value limit.
double max_out_limit;//Maximum allowable value or adjustment
double min_out_limit;//Minimum allowable value or adjustment
In fact I have two D terms in my PID. One is change in the sampled values (IE the delta term from sample n-1 to n) and the directly measured rate. The directly measured differential/change rates are from the IMU and GPS.
I'm currently working on the interface to selectively change these PID constants in flight. This might be easier if I switch to a two person operation, one to fly the helicopter and one to twiddle the gains. For Now I'm just going to work one axis/ PID at a time.
Above all of this is the rather simple executive that generates the sequence of target lat,lon and altitude. At this point that excutive just tried to freeze the vehicle in space when activated. (IE use the current Yaw, Alt ,Lat,Lon as the target)
(Sorry for the crummy code formatting blogger does not seem to like formatting code in a reasonable way)
My scheme for control is to use a set of PID loops.
Most likely some of these will only have P gain, but the concept is to use the following:(Copied from code) The PIDs marked with * in the comments will be different in the rocket.
OnePidElement Yaw_to_Rudder; //Takes IMU yaw and drives rudder *
OnePidElement Alt_to_VSpeed; // target altitude drives desired vspeed.
OnePidElement VSpeed_To_Collective;// desired vspeed drives collective.*
OnePidElement Pitch_To_Elevator;//desired pitch drives Elevator.*
OnePidElement Roll_To_Alieron;// desired roll drives Alieron.*
OnePidElement V_Forward_To_Pitch;//desired Vforward drives pitch.
OnePidElement V_Right_To_Roll; //desired Vright and drives roll
OnePidElement Long_to_V_East; //desired Longitude and drives VEast.
OnePidElement Lat_to_V_North; //desired Lattitude and drives VNorth;
And one more conversion function:
void ConvertDirection(double V_North, //Desired V_North input
double V_East,//Desired V_East input
double Yaw,//Current True YAW corrected for magnetic deviation input,
double &V_Forward,// Converted V_Forward target out
double & V_Right, //Converted V_Right target out
);
OnePidElement is an object that holds the a PIDGainConstants object and the current integration state.
The Yaw to rudder , Pitch to Elevator and Roll to Alieron PIDs will be run for each IMU sample.
All other PID's will be run for each GPS data set.
I'm not planning to integrate the accelerometers. (Yet)
An example would be:
Elevator=Pitch_To_Elevator.DoServoPidAdjust(target_pitch, imu.pitch , imu.x_rate);
Each OnePidElement contins a PID gainObject that has the following gain limit elements:
double p_gain;//Proportional Gain
double i_gain;//Integrator Gain;
double d_delta_gain; //Sample to Sample delta gain
double d_meas_gain; //Rate as measured by IMU or GPS
double max_i_windup;// Maximum integrator value limit.
double min_i_windup;//Minimum integrator value limit.
double max_out_limit;//Maximum allowable value or adjustment
double min_out_limit;//Minimum allowable value or adjustment
In fact I have two D terms in my PID. One is change in the sampled values (IE the delta term from sample n-1 to n) and the directly measured rate. The directly measured differential/change rates are from the IMU and GPS.
I'm currently working on the interface to selectively change these PID constants in flight. This might be easier if I switch to a two person operation, one to fly the helicopter and one to twiddle the gains. For Now I'm just going to work one axis/ PID at a time.
Above all of this is the rather simple executive that generates the sequence of target lat,lon and altitude. At this point that excutive just tried to freeze the vehicle in space when activated. (IE use the current Yaw, Alt ,Lat,Lon as the target)
(Sorry for the crummy code formatting blogger does not seem to like formatting code in a reasonable way)
Wednesday, January 16, 2008
The urge to have a science project.
One has to be careful that time and money are allocated correctly. For several years I've been contemplating developing a lower cost GPS Differential/RTK system using commercial receivers.
While an open source solution would be a nice to have, it really makes no sense. I can purchase off the shelf differential GPS solutions that are inexpensive given any realistic valuation of my time. Rather than spend months developing a GPS solution I've decided to just purchase one off the shelf. I'm going to use the hemisphere GPS crescent oem board with their RTK and 20 Hz options. I'll integrate the RTK base into my Telemetry suitcase and the rover goes on the Rocket/Helicopter. This is just so much easier than developing a either a GPS solution or a fancy interial/GPS Kalman filter. The data sheet accuracy for the RTK solution is 2cm. If it can keep that in a dynamic environment that will be amazing, even the specified L-diff solution at 28cm is plenty good enough.
While an open source solution would be a nice to have, it really makes no sense. I can purchase off the shelf differential GPS solutions that are inexpensive given any realistic valuation of my time. Rather than spend months developing a GPS solution I've decided to just purchase one off the shelf. I'm going to use the hemisphere GPS crescent oem board with their RTK and 20 Hz options. I'll integrate the RTK base into my Telemetry suitcase and the rover goes on the Rocket/Helicopter. This is just so much easier than developing a either a GPS solution or a fancy interial/GPS Kalman filter. The data sheet accuracy for the RTK solution is 2cm. If it can keep that in a dynamic environment that will be amazing, even the specified L-diff solution at 28cm is plenty good enough.
Tuesday, January 15, 2008
A Quick test flight.
I fully checked out the power system and added a completely 100% separate regulator for the receiver. I re did the bearings in the blade grips and I then flew the helicopter this morning before work. The flight was uneventful. I left the telemetry receiver sitting in the front seat of the truck and this caused telemetry dropouts. Up to now the telemetry reception has been 100% perfect. The display software was ignoring the checksums and size checks, after todays flight I need to fix that as partial data frames make for really strange data. This will be tonights task. The next test flight will test altitude hold.
P.S. any GPS internals experts out there reading the blog? I would like to put together a low cost open source L1 code differential solution and or carrier phase RTK solution. I think this would be a very valuable tool for a lot of interesting robot, uav, helicopter, rocket etc... projects.
I even willing to subsidize the effort with some $.
P.S. any GPS internals experts out there reading the blog? I would like to put together a low cost open source L1 code differential solution and or carrier phase RTK solution. I think this would be a very valuable tool for a lot of interesting robot, uav, helicopter, rocket etc... projects.
I even willing to subsidize the effort with some $.
Sunday, January 13, 2008
(Update) A Day of testing.
(Update I found the receiver problem, read to end)
I drove out to Mojave Friday night and spent all day Saturday at FAR. There was a TV program shooting pictures of large high power rockets and that was kind of cool to watch. It took them all day to do some background video and two flights. The flights went perfectly. I had often contemplated inviting some TV to our tests, but after watching them all day I don't think I could handle the time impact, its much more intrusive than I would have expected.
In any case I set up shop in the propellant mixing shed and did some flight testing. My previous helicopter testing I'd writte some code, drive somewhere to test it, go home to review the data and do it again. Saturday I had the laptop in a reasonably comfortable dim space 10 steps from where I could fly the helicopter. (Dim is necessary because you can't really read a laptop in bright sun). I made a lot more progress than I would have the traditional way. It was really nice to be able to change code do a 30 second flight review data and then change code again all inside 10 minutes. It was not perfect, the smallest screen I usually do development on is a nice 24" LCD. Doing development on the laptop fees cramped, but the quick cycle time is a big win.
Flight #1I verified that the CCPM code on the helicopter worked correctly in flight. I also verified that the heading hold code developed on the lazy susan works properly in flight.
Flight #2 I fixed the heading hold gain and removed it from the adjustable gain lever in preparation for doing altitude hold. I also did some hard vertical climbs and descents to gather some altitude data. On review the GPS altitude data was really choppy. I added an integration of the GPS velocity to the variables calculated and modified the data review code to allow me to zero this and display it. (The display code is a lot more complicated than the flight code and hence harder top work with on the Laptop)
Flight #3 Integrated GPS velocity was much better, still not perfect, the data had a downward bias. Sat down and looked carefully at the GPS data, GPS altitude was jumping in 4 m steps, very strange. I had not yet looked at the GPS position data, it looks reasonable, but Id not carefully examined it. So I paced off a 20M square oriented to true norht in the dirt and marked the corners.
Hand carry #1 I then carefully hand carried the helicopter over the 20 M square. First at waist height, then with the helicopter held as high as I could over my head. On review I got zero data. So I swap out the sd card in the data logger and do a 30 second run .I got data this time. A note on the data collection process. The Laptop can display all the data in real time, but the useful mode is to command the telmetry suitcase to shut down. Take the SD card out of the telemetry suitcase, put it into the reader, copy it into the laptop data directory, rename it to something meaningful, and write a summary in the lab notebook of what the flight test was while you still remember, then review the data on the laptop. I need to streamline this process.
Hand Carry #2
I carrnyone watching would think I'd gone crazy and was out waltzing with my helicopter. On review thy the helicopter around the 20 m square spinning 360 degrees at each corner (so I can see the heading change on the data to know where the corners were.) Ae GPS position data just isn't right. The altitude data is also doing 4M jumps. Only the GPS data is suspect, everything else is fine. The GPS data goes from the GPS to the onboard computer in binary form then its converted to be computer endian and packaged into another structure and set out telemetry. So I add another telemetry frame type to ship the raw unconverted GPS binary data to down the telemetry stream without touching it at all. I then modify the data display program to have duplicate fields for all the GPS data. (The PC is the same endian as the GPS no conversion necessary).
Hand Carry #3 Same path around the 20M square spinning at each corner.The two data sets do not AGREE!!!!! ARGHHHH. In looking at the endian conversion on the PC telemetry side I'd used HTONL host to network long it works as expected because the PC does not store data in the expected network byte order. On the Netburner side the natural storage is network byte order so HTONL is a no op on the platform. SO I'd written my own byte swap. It had typo/ error, where the 3rd byte of the float got the 4th byte duplicated. On the 8 byte doubles the 3rd got the 4th and the 7th got the 8th. So I fix this.
Hand Carry #4 The Data sets match, and the altitude is sensitive enough and not jumpy. It even detects me setting the helicopter on the ground , on the work table and holding it over my head! Cool.
Flight #4 Lift off and the helicopter is shaking/ vibrating really badly. Land immediately. One tail rotor blade had split, probably hit the sand on the flight #3 landing. Change tail rotor blades.
Flight 6.7.8.9.10.11 etc... Helicopter is still vibrating, main blade tracking is really off. I do a short flight and try to adjust the tracking. I have some people trying to help me spot which blade is high the red or blue tip. The tracking just seems random, either I'm making to big adjustment or something else is wrong. Still vibrating badly. On the 6th or 7th hop helicopter goes from low hover down to land abruptly, not damaging hard, but more abrupt, and uncommanded by me.
Helicopter is sitting on the ground upright and running and I have no control. Thats easy I've set up so the motor controller is not run by my computer system it's run directly by the RC receiver so in the worst case I can shut it down without relying on software. no dice, the system does not shutdown???? I continue to fiddle with the transmitter, I shut it off. (RC receiver failsafe should shut it down... it does not) Flip the transmitter on and off. Walk around the helicopter trying fiddeling with the transmitter. It shuts down. Quickly go over and disconnect the main power battery. Back on the work bench table I test the receiver battery pack and it seems very low. All the parts of the rotor head seem ok, so I suspect that the rotor blades are failing in some way. I remove the rotor baldes and run the helicopter on the bench. Very smooth and no vibration. I take my spare blades and using a sharpie paint a black stripe on one tip. I install a fresh receiver battery and the new blades. All the controls work, I check all the cable bundels for a loose connector or other problem. All looks good.
Flight N+1 I set the helicopter down on the ground and command the motor to start. I immediately loose control. The Motor is running the helicopter has negative collective commanded so its firmly on the ground but I have no control. I start fiddeling with the transmitter on-off nothing the helicopter will not shut down. After about 5 minutes of this I crawl up to the front of the helicopter reach in and disconnect the power battery.
Is it the transmitter or the receiver?
I take out the small Trex 450 and fly it, it's perfect. The problem is not the transmitter.
Start packing up. I put everything away tables back in my container. Clean up pack etc.
I pack up everything but the little Trex. So I fly that some just for fun. I did my first helicopter rolls in real life!. I've done them on the simulator a lot, but this was the first time in real life. I pack up. Its 4:45 pm I arrive back home at 9:30 PM (Traffic in LA was bad) I unpack the car. All in all a great day.
I suspect that my receiver problem is related to this.
I apologize to all that this has become the unreasonable helicopter blog. But we should be back to rockets in the next 4 to 6 weeks.
I did some more testing today outside the garage. The on/off stick on problem persists even
when I changed the receiver. It goes away if I power the receiver separately.It seems that there is a loose or flaky power problem with the system. I'm going to put the receiver on a separate power source. I also rebuilt the bearings in the blade grips and replaced the plastic blade grips with metal and now the rotor tracks perfectly. In any case I now have a spare receiver and I've done the rework recommended in the link to my earlier suspected problem.
I drove out to Mojave Friday night and spent all day Saturday at FAR. There was a TV program shooting pictures of large high power rockets and that was kind of cool to watch. It took them all day to do some background video and two flights. The flights went perfectly. I had often contemplated inviting some TV to our tests, but after watching them all day I don't think I could handle the time impact, its much more intrusive than I would have expected.
In any case I set up shop in the propellant mixing shed and did some flight testing. My previous helicopter testing I'd writte some code, drive somewhere to test it, go home to review the data and do it again. Saturday I had the laptop in a reasonably comfortable dim space 10 steps from where I could fly the helicopter. (Dim is necessary because you can't really read a laptop in bright sun). I made a lot more progress than I would have the traditional way. It was really nice to be able to change code do a 30 second flight review data and then change code again all inside 10 minutes. It was not perfect, the smallest screen I usually do development on is a nice 24" LCD. Doing development on the laptop fees cramped, but the quick cycle time is a big win.
Flight #1I verified that the CCPM code on the helicopter worked correctly in flight. I also verified that the heading hold code developed on the lazy susan works properly in flight.
Flight #2 I fixed the heading hold gain and removed it from the adjustable gain lever in preparation for doing altitude hold. I also did some hard vertical climbs and descents to gather some altitude data. On review the GPS altitude data was really choppy. I added an integration of the GPS velocity to the variables calculated and modified the data review code to allow me to zero this and display it. (The display code is a lot more complicated than the flight code and hence harder top work with on the Laptop)
Flight #3 Integrated GPS velocity was much better, still not perfect, the data had a downward bias. Sat down and looked carefully at the GPS data, GPS altitude was jumping in 4 m steps, very strange. I had not yet looked at the GPS position data, it looks reasonable, but Id not carefully examined it. So I paced off a 20M square oriented to true norht in the dirt and marked the corners.
Hand carry #1 I then carefully hand carried the helicopter over the 20 M square. First at waist height, then with the helicopter held as high as I could over my head. On review I got zero data. So I swap out the sd card in the data logger and do a 30 second run .I got data this time. A note on the data collection process. The Laptop can display all the data in real time, but the useful mode is to command the telmetry suitcase to shut down. Take the SD card out of the telemetry suitcase, put it into the reader, copy it into the laptop data directory, rename it to something meaningful, and write a summary in the lab notebook of what the flight test was while you still remember, then review the data on the laptop. I need to streamline this process.
Hand Carry #2
I carrnyone watching would think I'd gone crazy and was out waltzing with my helicopter. On review thy the helicopter around the 20 m square spinning 360 degrees at each corner (so I can see the heading change on the data to know where the corners were.) Ae GPS position data just isn't right. The altitude data is also doing 4M jumps. Only the GPS data is suspect, everything else is fine. The GPS data goes from the GPS to the onboard computer in binary form then its converted to be computer endian and packaged into another structure and set out telemetry. So I add another telemetry frame type to ship the raw unconverted GPS binary data to down the telemetry stream without touching it at all. I then modify the data display program to have duplicate fields for all the GPS data. (The PC is the same endian as the GPS no conversion necessary).
Hand Carry #3 Same path around the 20M square spinning at each corner.The two data sets do not AGREE!!!!! ARGHHHH. In looking at the endian conversion on the PC telemetry side I'd used HTONL host to network long it works as expected because the PC does not store data in the expected network byte order. On the Netburner side the natural storage is network byte order so HTONL is a no op on the platform. SO I'd written my own byte swap. It had typo/ error, where the 3rd byte of the float got the 4th byte duplicated. On the 8 byte doubles the 3rd got the 4th and the 7th got the 8th. So I fix this.
Hand Carry #4 The Data sets match, and the altitude is sensitive enough and not jumpy. It even detects me setting the helicopter on the ground , on the work table and holding it over my head! Cool.
Flight #4 Lift off and the helicopter is shaking/ vibrating really badly. Land immediately. One tail rotor blade had split, probably hit the sand on the flight #3 landing. Change tail rotor blades.
Flight 6.7.8.9.10.11 etc... Helicopter is still vibrating, main blade tracking is really off. I do a short flight and try to adjust the tracking. I have some people trying to help me spot which blade is high the red or blue tip. The tracking just seems random, either I'm making to big adjustment or something else is wrong. Still vibrating badly. On the 6th or 7th hop helicopter goes from low hover down to land abruptly, not damaging hard, but more abrupt, and uncommanded by me.
Helicopter is sitting on the ground upright and running and I have no control. Thats easy I've set up so the motor controller is not run by my computer system it's run directly by the RC receiver so in the worst case I can shut it down without relying on software. no dice, the system does not shutdown???? I continue to fiddle with the transmitter, I shut it off. (RC receiver failsafe should shut it down... it does not) Flip the transmitter on and off. Walk around the helicopter trying fiddeling with the transmitter. It shuts down. Quickly go over and disconnect the main power battery. Back on the work bench table I test the receiver battery pack and it seems very low. All the parts of the rotor head seem ok, so I suspect that the rotor blades are failing in some way. I remove the rotor baldes and run the helicopter on the bench. Very smooth and no vibration. I take my spare blades and using a sharpie paint a black stripe on one tip. I install a fresh receiver battery and the new blades. All the controls work, I check all the cable bundels for a loose connector or other problem. All looks good.
Flight N+1 I set the helicopter down on the ground and command the motor to start. I immediately loose control. The Motor is running the helicopter has negative collective commanded so its firmly on the ground but I have no control. I start fiddeling with the transmitter on-off nothing the helicopter will not shut down. After about 5 minutes of this I crawl up to the front of the helicopter reach in and disconnect the power battery.
Is it the transmitter or the receiver?
I take out the small Trex 450 and fly it, it's perfect. The problem is not the transmitter.
Start packing up. I put everything away tables back in my container. Clean up pack etc.
I pack up everything but the little Trex. So I fly that some just for fun. I did my first helicopter rolls in real life!. I've done them on the simulator a lot, but this was the first time in real life. I pack up. Its 4:45 pm I arrive back home at 9:30 PM (Traffic in LA was bad) I unpack the car. All in all a great day.
I suspect that my receiver problem is related to this.
I apologize to all that this has become the unreasonable helicopter blog. But we should be back to rockets in the next 4 to 6 weeks.
I did some more testing today outside the garage. The on/off stick on problem persists even
when I changed the receiver. It goes away if I power the receiver separately.It seems that there is a loose or flaky power problem with the system. I'm going to put the receiver on a separate power source. I also rebuilt the bearings in the blade grips and replaced the plastic blade grips with metal and now the rotor tracks perfectly. In any case I now have a spare receiver and I've done the rework recommended in the link to my earlier suspected problem.
Thursday, January 10, 2008
Data Review.
I modified the data display software tonight to back out the Collective, Pitch and Roll commands from the CCPM servo data. I then reviewed the free flights I did on the 3rd. Toward the end of the flight I did deliberate abrupt pitch, roll and climb maneuvers so I could look at the data and see how much servo movement corresponded with how much vehicle movement. The picture below is a screen capture of the data display. Sevro Roll is the Roll command (red) Roll (Blue) is the actual vehicle roll and the ragged (magenta) line is the raw measured gyro rate.
They all look reasonable. As did pitch , servo pitch and X rate. The Vertical velocity tracked collective reasonable well, but the altitude seemed to wander a lot more. Click on the picture for a bigger view.
Its 11:00 pm and this was another 4 1/2 hour evening.
They all look reasonable. As did pitch , servo pitch and X rate. The Vertical velocity tracked collective reasonable well, but the altitude seemed to wander a lot more. Click on the picture for a bigger view.
Its 11:00 pm and this was another 4 1/2 hour evening.
Fly as you train, train as you fly.
I've been flying RC airplanes for a very long time, but I did not ever fly a helicopter until about two years ago. I bought the real flight simulator and made a serious, 15 minutes an evening , effort to learn to fly the helicopter. I did this every evening for months. I did not buy a helicopter until I could fly the simulator with full realism and gusty wind 10 times out of ten for A full tank of gas without crashing. Once I could do 10 of 10 I bought a helicopter jkit and started trying to fly in the real world. This illustrates a subtle point the picture below shows me sitting in my computer chair flying the sim.
The only problem is that if you then take a picture of me holding the real transmitter
like I fly the real helicopter there are differences.
With the transmitter on my lap I hold the sticks with my fingers, standing with the tranmitter dangling I naturally fly with my thumbs. On the simulator I can easily do 720 degree piroettes
without out gaining or loosing altitude ot position stability. I real life this is not so easy.
So I've started practicing with the simulator standing in front of the computer with the simulator controller hanging from a strap. Even subtle differences between things make a difference. Especially if it is in trained muscle memory.
The next helicopter Step.
Basic control laws are going to be:
1)Desired course/way points ->generates desired position.
2)Current position(gps) and desired position ->Generate desired velocity.
3)Desired velocity +Actual velocity(gps) ->Generate desired pitch/roll attitude.
4)Desired Pitch Roll Attitude +Actual pitch roll attitude(imu) -> Generate (virtual) Elevator and Aileron signals.
Separately we control heading (alwayas points true north) and altitude. (Heading control is done and works)
Note that all of thsi software will be identical on the rocket, except the very last part
>>>Desired Pitch Roll Attitude +Actual pitch roll attitude -> Generate Elevator and Aileron signals.
I've had all this working with the helicopter simulator for 6 or more months. I'm just a bit cautious and chicken when it comes to flying it in the real helicopter. I'm going to work my way up the list backwards. This brings me to todays waffling decision. As presently set up the helicopter is about 4K of hardware and 100 hours of work. I'm a bit cautious with it.
I worked out the yaw control with a lazy Susan. Today I gathered all the parts necessary to
build a mount for the helicopter that would allow it to move about 15 degrees
in pitch and roll and 360 degrees in yaw freely. It would take me about 4 hours to assemble all of this. This only helps with Step 4 all the other steps have to be done in free flight anyway, so is it worth building the pivot mount??? My strategy is as follows Beyond the basic flight controls I have the software set up to respond to two of the RC transmitter controls (outlined in red below)
Aux 2 is a three position switch that selects three software modes. 0,1,2
Mode 0 is full manual control.
Mode 1 enables the autopilot parts that presently work. (currently only the yaw)
Mode 2 enables the new component we want to test.
"Lever" is a slide lever on the side of the helicopter that I have setup to control a software
variable that goes from 0 to 100. The intent is to have this lever control the gain of the control loop I'm currently working on. The problem is that both of these are on the wrong side of the transmitter for the next step as the cyclic control is what I'm trying to automate and also the right hand stick. My real problem is that I actually need to start flying the helicopter regularly.
I also do most of my work in the evening so I need to fly it at night and its not safe to fly by myself. (The big Trex600 could cause serious injury if it went out of control and went for the pilot) I've flown the vehicle a couple of times in the dirt parking lot near the DelMar fairgrounds
(The security guard thought the helicopter was cool, but told me that if anyone asks I'm not supposed to be there.) I could start flying at one of the regular RC model flying clubs, but the fact that the system has a GPS and could, with the proper software, fly beyond the pilots direct line of sight makes in in violation of the RC club safety rules. I think it would be rude to jeopardize a long standing RC club and its flying field by violating the rules.
The only problem is that if you then take a picture of me holding the real transmitter
like I fly the real helicopter there are differences.
With the transmitter on my lap I hold the sticks with my fingers, standing with the tranmitter dangling I naturally fly with my thumbs. On the simulator I can easily do 720 degree piroettes
without out gaining or loosing altitude ot position stability. I real life this is not so easy.
So I've started practicing with the simulator standing in front of the computer with the simulator controller hanging from a strap. Even subtle differences between things make a difference. Especially if it is in trained muscle memory.
The next helicopter Step.
Basic control laws are going to be:
1)Desired course/way points ->generates desired position.
2)Current position(gps) and desired position ->Generate desired velocity.
3)Desired velocity +Actual velocity(gps) ->Generate desired pitch/roll attitude.
4)Desired Pitch Roll Attitude +Actual pitch roll attitude(imu) -> Generate (virtual) Elevator and Aileron signals.
Separately we control heading (alwayas points true north) and altitude. (Heading control is done and works)
Note that all of thsi software will be identical on the rocket, except the very last part
>>>Desired Pitch Roll Attitude +Actual pitch roll attitude -> Generate Elevator and Aileron signals.
I've had all this working with the helicopter simulator for 6 or more months. I'm just a bit cautious and chicken when it comes to flying it in the real helicopter. I'm going to work my way up the list backwards. This brings me to todays waffling decision. As presently set up the helicopter is about 4K of hardware and 100 hours of work. I'm a bit cautious with it.
I worked out the yaw control with a lazy Susan. Today I gathered all the parts necessary to
build a mount for the helicopter that would allow it to move about 15 degrees
in pitch and roll and 360 degrees in yaw freely. It would take me about 4 hours to assemble all of this. This only helps with Step 4 all the other steps have to be done in free flight anyway, so is it worth building the pivot mount??? My strategy is as follows Beyond the basic flight controls I have the software set up to respond to two of the RC transmitter controls (outlined in red below)
Aux 2 is a three position switch that selects three software modes. 0,1,2
Mode 0 is full manual control.
Mode 1 enables the autopilot parts that presently work. (currently only the yaw)
Mode 2 enables the new component we want to test.
"Lever" is a slide lever on the side of the helicopter that I have setup to control a software
variable that goes from 0 to 100. The intent is to have this lever control the gain of the control loop I'm currently working on. The problem is that both of these are on the wrong side of the transmitter for the next step as the cyclic control is what I'm trying to automate and also the right hand stick. My real problem is that I actually need to start flying the helicopter regularly.
I also do most of my work in the evening so I need to fly it at night and its not safe to fly by myself. (The big Trex600 could cause serious injury if it went out of control and went for the pilot) I've flown the vehicle a couple of times in the dirt parking lot near the DelMar fairgrounds
(The security guard thought the helicopter was cool, but told me that if anyone asks I'm not supposed to be there.) I could start flying at one of the regular RC model flying clubs, but the fact that the system has a GPS and could, with the proper software, fly beyond the pilots direct line of sight makes in in violation of the RC club safety rules. I think it would be rude to jeopardize a long standing RC club and its flying field by violating the rules.
Wednesday, January 09, 2008
Another evenings Details.
I picked up burger king on the way home, I got home at about 6:30. Mariellen (my wife) is still fighting the cold/flu. when she is feeling bad she naps all day. She had already eaten so I finished dinner and watched news at about 7:00.
I really liked the way the lazy susan worked for the rudder so after thinking about it I thought the concept might be useful for pitch and roll. I'm thinking I'll mount the helicopter on top of some kind of post with a ball joint so it can pitch roll and spin. So I start the evening with the McMastercarr website looking for a good ball joint. I find several, they are either 2 weeks lead or in stock in Chicago. (anything in stock in Los Angles is next day even when paying UPS ground charges)
I want to do this this week end so I either pay next day air charges or find a different solution.
I have until Thursday Morning to decide so I go out in the garage open up my Mechanical junk box and start digging. I find the jewel like hand made ball bearing universal joint mounted to an estes D motor with some digital servos. A long ago experiment that I machined up only to discover that the inertia moments for a small rocket mean you need really fast response. Faster than the servos can give. I disassemble this assembly (It was about 20 hours of jewel like machining on the taig CNC mill three years ago.) It looks strong enough, but the range of motion is limited and no rotation. So I keep digging and find a large Rod end with a ball bearing that will be perfect. I just need to get the right kind of spacers and through bolt from Marshals Industrial Hardware Thursday at Lunch. I clean up my mechanical parts mess and go back in the house. Time 8:30. I check up on Mariellen, she is still feeling yucky, but she needs some things at the store. Trip to store return at about 9:00.
Next Stop helicopter software.
The helicopter uses CCPM Cyclic Collective Pitch mixing. What does this mean?
A normal single rotor helicopter has three main controls. The Tail rotor pitch for Yaw or turning left right. Collective pitch for changing the amount of lift. Collective pitch controls the main rotor blade pitch collectively, meaning all the blades increase or decrease pitch together.
The cyclic pitch control for tipping in pitch forward/back, or and roll left/right. Cyclic pitch cyclically changes the blade pitch as it goes around. All of this is transmitted to the rotor blade via the swashplate. The swash moves up and down for collective and tips forward/ back left/right for cyclic control.
The traditional method for controlling the swash is to have separate controls, or actuators for pitch, roll and collective and to mix them together with a mechanical mixing system. Every added linkage ads slop to the controls. The mechanical mixing systems add lots of slop. The acrobatic RC helicopter guys figured out that if you connect the servos directly to the swash plate, with no other linkages, things would be more precise. So they invented CCPM what it really means is that there are three servos spaced evenly around the swash plate at 120 degree intervals. If you want the swash to go straight up for a pure collective move then all three servos have to move straight up. If you want the swash to roll to the left, the rear servo stays still, the left goes down and the right goes up. It you want it to pitch nose up, the rear servo goes down and the left- right servos go up, but by half the amount. cos( 120 degrees/2). All of this is normally handled by some software in the RC transmitter. the way I'm currently flying is to just read the commanded positions and have the computer pass them through without modification. (Other than the rudder where I have compass heading hold working when commanded)
I really want to start working on the pitch, roll and collective controls. So rather than debug my mixing software at the same time as my controls software I split the beast in half. I'll tell the RC transmitter to treat the helicopter like it has mechanical mixing and have the software do the CCPM mixing on the helicopter.
Step 1) Backup ALL the software everywhere into a was_working_1_09_08 directory.
Step 2) remove the helicopter from the Lazy Susan and bring it inside to test.
Step 3) Modify the Telemetry display software so it shows servo pulse positions in counts rather than +/-100%
Step 4 )Run the existing system and record all the servo (right, left, rear) positions for:
Full down and Full up and neutral collective with neutral cyclic.
Full forward, Aft and neutral cyclic with neutral collective.
Step 5)Reprogram the transmitter to not do CCPM. *(requires downloading manual from JR website and reading a few pages)
Step 6)Record the servo count limits for Elevator, Aileron and Collective servos.
Step 7 )put all the numbers from step 4 and 6 into excel and see if the make sense. They do make sense. The scalings all look reasonable and linear.
Step 8) Reconfigure software to store received RC commands from the appropriate channels in Collective, Aileron and Elevator variables.
Step 9 )write code to translate these Collective, Aileron and Elevator variables into servo commands for left, right and rear. (remembering to limit check everything)
Step 10) Test the software.
I finished this at about 10:30, but by this time the helicopter had been running controls and telemetry non stop for 1.5 hours and the status indicators were giving me the controls battery too low indications. I still need to repeat step 4 with the new software to make sure my mapping is correct, but it looks good visually. I'll do that in the morning before I go to work.
It's currently 11:01 another evening gonI e. I have to stay up until the battery is done as I don't leave LiPos on a charger unattended. ( I wrote this entry while the battery was on the charger.)
I also need to go to bed. Its going to be a long day at work Thursday as my business partner and one of by best support engineers are going to CES to gawk at the 150 inch LCD screens.
This means I'll have to do a bit more than normal in both sales support and technical support.
I really liked the way the lazy susan worked for the rudder so after thinking about it I thought the concept might be useful for pitch and roll. I'm thinking I'll mount the helicopter on top of some kind of post with a ball joint so it can pitch roll and spin. So I start the evening with the McMastercarr website looking for a good ball joint. I find several, they are either 2 weeks lead or in stock in Chicago. (anything in stock in Los Angles is next day even when paying UPS ground charges)
I want to do this this week end so I either pay next day air charges or find a different solution.
I have until Thursday Morning to decide so I go out in the garage open up my Mechanical junk box and start digging. I find the jewel like hand made ball bearing universal joint mounted to an estes D motor with some digital servos. A long ago experiment that I machined up only to discover that the inertia moments for a small rocket mean you need really fast response. Faster than the servos can give. I disassemble this assembly (It was about 20 hours of jewel like machining on the taig CNC mill three years ago.) It looks strong enough, but the range of motion is limited and no rotation. So I keep digging and find a large Rod end with a ball bearing that will be perfect. I just need to get the right kind of spacers and through bolt from Marshals Industrial Hardware Thursday at Lunch. I clean up my mechanical parts mess and go back in the house. Time 8:30. I check up on Mariellen, she is still feeling yucky, but she needs some things at the store. Trip to store return at about 9:00.
Next Stop helicopter software.
The helicopter uses CCPM Cyclic Collective Pitch mixing. What does this mean?
A normal single rotor helicopter has three main controls. The Tail rotor pitch for Yaw or turning left right. Collective pitch for changing the amount of lift. Collective pitch controls the main rotor blade pitch collectively, meaning all the blades increase or decrease pitch together.
The cyclic pitch control for tipping in pitch forward/back, or and roll left/right. Cyclic pitch cyclically changes the blade pitch as it goes around. All of this is transmitted to the rotor blade via the swashplate. The swash moves up and down for collective and tips forward/ back left/right for cyclic control.
The traditional method for controlling the swash is to have separate controls, or actuators for pitch, roll and collective and to mix them together with a mechanical mixing system. Every added linkage ads slop to the controls. The mechanical mixing systems add lots of slop. The acrobatic RC helicopter guys figured out that if you connect the servos directly to the swash plate, with no other linkages, things would be more precise. So they invented CCPM what it really means is that there are three servos spaced evenly around the swash plate at 120 degree intervals. If you want the swash to go straight up for a pure collective move then all three servos have to move straight up. If you want the swash to roll to the left, the rear servo stays still, the left goes down and the right goes up. It you want it to pitch nose up, the rear servo goes down and the left- right servos go up, but by half the amount. cos( 120 degrees/2). All of this is normally handled by some software in the RC transmitter. the way I'm currently flying is to just read the commanded positions and have the computer pass them through without modification. (Other than the rudder where I have compass heading hold working when commanded)
I really want to start working on the pitch, roll and collective controls. So rather than debug my mixing software at the same time as my controls software I split the beast in half. I'll tell the RC transmitter to treat the helicopter like it has mechanical mixing and have the software do the CCPM mixing on the helicopter.
Step 1) Backup ALL the software everywhere into a was_working_1_09_08 directory.
Step 2) remove the helicopter from the Lazy Susan and bring it inside to test.
Step 3) Modify the Telemetry display software so it shows servo pulse positions in counts rather than +/-100%
Step 4 )Run the existing system and record all the servo (right, left, rear) positions for:
Full down and Full up and neutral collective with neutral cyclic.
Full forward, Aft and neutral cyclic with neutral collective.
Step 5)Reprogram the transmitter to not do CCPM. *(requires downloading manual from JR website and reading a few pages)
Step 6)Record the servo count limits for Elevator, Aileron and Collective servos.
Step 7 )put all the numbers from step 4 and 6 into excel and see if the make sense. They do make sense. The scalings all look reasonable and linear.
Step 8) Reconfigure software to store received RC commands from the appropriate channels in Collective, Aileron and Elevator variables.
Step 9 )write code to translate these Collective, Aileron and Elevator variables into servo commands for left, right and rear. (remembering to limit check everything)
Step 10) Test the software.
I finished this at about 10:30, but by this time the helicopter had been running controls and telemetry non stop for 1.5 hours and the status indicators were giving me the controls battery too low indications. I still need to repeat step 4 with the new software to make sure my mapping is correct, but it looks good visually. I'll do that in the morning before I go to work.
It's currently 11:01 another evening gonI e. I have to stay up until the battery is done as I don't leave LiPos on a charger unattended. ( I wrote this entry while the battery was on the charger.)
I also need to go to bed. Its going to be a long day at work Thursday as my business partner and one of by best support engineers are going to CES to gawk at the 150 inch LCD screens.
This means I'll have to do a bit more than normal in both sales support and technical support.
Tuesday, January 08, 2008
What does it take...
My Son is currently working on an interesting business idea with some friends up in the bay area. So I'm currently working on the project solo. What does this mean?
I'll give you a brief rundown of just this evening. (A fairly typical evening.)
I got home from work about 5:45.
I usually sit down and have dinner with my wife and who ever is here.
My Wife is battling a cold (the one I had last week) so she was asleep so I heated up some soup in the microwave and watched the NH election returns while I ate dinner.
6:15 out to the garage.
I'm trying to get a handle on valves so I pull out all the sample valves and actuators I've collected to look at them. I think I want to concentrate on the brush less actuator and the Dynamixl actuators.
One of the possible valves is a cyro rated globe valve, but it takes multiple turns.
The torque of the brush less actuator is insane with the 256:1 gear box, but I need faster if I'm going to use a multi turn valve. So I remove the brushless motor from the 2656:1 and put it on the 36:1 gear box. This involves removing one very stubborn screw and machining two parts on the lathe. Elapsed time 2 hrs its now 8:15. On the 36:1 gearbox the brushless actuator is still stronger than I need. however the actuator speed is not symmetrical, the brush less controller still thinks its driving a car, not a servo. So go dig through the manuals files looking for the programming instructions for the Novak "goat" brush less controller. After decoding their programming scheme with 4 multicolor blinking lights and a single button I have the controller operating in servo mode. Still insanely strong and veryfast. It looks like a good possibility.
Next I move on to the next actuator, the Dynamixel RX-64.
I go to the computer and download and print the manual. I review the specs and discover that the claimed max torque is the same as the much bigger, beefier and heavier tonegowa, cool,
I knew it was good, but my mental model had it half that strong, My head stores data in a variety of units and I messed up the mental Kgcm to inoz conversion in making that assumption.
Now to make it work. Step one build a wiring harness, first problem the manual talks about 5 pins, the connectors and cables only have 4????
After some head scratching I see that the case and semi-hidden PCB have 5 pins, but the connector soldered in is only 4 pins. mystery solved. Get up from the computer go out to the garage and set up the soldering iron and heat shrink gun and make a nice cable.
Now what to connect the actuator to for testing? It needs RS-485 half duplex, so I dig through my NetBurner junk box and find a carrier board that supports RS-485 half duplex.
Next I dig up the schematic for the obsolete carrier board (The obsolete stuff comes home, the new stuff gets sold.) and wire up the RS-485. I haven't done any RS-485 programming in awhile, so I haul out the scope to make sure the enable disable timing is correct. It is,so
now I have to figure out what the default baud rate is. The dynamixel manual tries very hard to hide this important bit of information but I hunt it down. In a few more minutes I have the actuator exchanging packets with me and giving me its internal temperature and status.
I just can't seem to get it to move....
Alas I have to enable "torque" and realize that the internal position commands are of a different endian state than what I was passing. The actuator moves and I can command it back and forth. Its reasonably fast and seems very strong. Cool! that only took 2 additional hours.
So I spent in excess of 5 hours this evening and I accomplished:
Changed gearbox on a possible actuator.
Verified that the dynamixels do what they say they do.
Wrote up this blog entry.
I usually take one evening a week and go do something with my wife like go to a movie or play. I usually take one evening to just vegetate. Other than that I'm usually woring on the rocket project. Only 10 months til LLC 2008, not nearly enough time.
I'll give you a brief rundown of just this evening. (A fairly typical evening.)
I got home from work about 5:45.
I usually sit down and have dinner with my wife and who ever is here.
My Wife is battling a cold (the one I had last week) so she was asleep so I heated up some soup in the microwave and watched the NH election returns while I ate dinner.
6:15 out to the garage.
I'm trying to get a handle on valves so I pull out all the sample valves and actuators I've collected to look at them. I think I want to concentrate on the brush less actuator and the Dynamixl actuators.
One of the possible valves is a cyro rated globe valve, but it takes multiple turns.
The torque of the brush less actuator is insane with the 256:1 gear box, but I need faster if I'm going to use a multi turn valve. So I remove the brushless motor from the 2656:1 and put it on the 36:1 gear box. This involves removing one very stubborn screw and machining two parts on the lathe. Elapsed time 2 hrs its now 8:15. On the 36:1 gearbox the brushless actuator is still stronger than I need. however the actuator speed is not symmetrical, the brush less controller still thinks its driving a car, not a servo. So go dig through the manuals files looking for the programming instructions for the Novak "goat" brush less controller. After decoding their programming scheme with 4 multicolor blinking lights and a single button I have the controller operating in servo mode. Still insanely strong and veryfast. It looks like a good possibility.
Next I move on to the next actuator, the Dynamixel RX-64.
I go to the computer and download and print the manual. I review the specs and discover that the claimed max torque is the same as the much bigger, beefier and heavier tonegowa, cool,
I knew it was good, but my mental model had it half that strong, My head stores data in a variety of units and I messed up the mental Kgcm to inoz conversion in making that assumption.
Now to make it work. Step one build a wiring harness, first problem the manual talks about 5 pins, the connectors and cables only have 4????
After some head scratching I see that the case and semi-hidden PCB have 5 pins, but the connector soldered in is only 4 pins. mystery solved. Get up from the computer go out to the garage and set up the soldering iron and heat shrink gun and make a nice cable.
Now what to connect the actuator to for testing? It needs RS-485 half duplex, so I dig through my NetBurner junk box and find a carrier board that supports RS-485 half duplex.
Next I dig up the schematic for the obsolete carrier board (The obsolete stuff comes home, the new stuff gets sold.) and wire up the RS-485. I haven't done any RS-485 programming in awhile, so I haul out the scope to make sure the enable disable timing is correct. It is,so
now I have to figure out what the default baud rate is. The dynamixel manual tries very hard to hide this important bit of information but I hunt it down. In a few more minutes I have the actuator exchanging packets with me and giving me its internal temperature and status.
I just can't seem to get it to move....
Alas I have to enable "torque" and realize that the internal position commands are of a different endian state than what I was passing. The actuator moves and I can command it back and forth. Its reasonably fast and seems very strong. Cool! that only took 2 additional hours.
So I spent in excess of 5 hours this evening and I accomplished:
Changed gearbox on a possible actuator.
Verified that the dynamixels do what they say they do.
Wrote up this blog entry.
I usually take one evening a week and go do something with my wife like go to a movie or play. I usually take one evening to just vegetate. Other than that I'm usually woring on the rocket project. Only 10 months til LLC 2008, not nearly enough time.
Monday, January 07, 2008
Valves....
If I stay with the four engine system the Swagelock plug valves are almost perfect for pressurization and fuel. (Won't work for Lox they freeze) One is shown below next to two dynamixel actuators.
These dynamixel actuators are robot servos with a an RS-485 interface will full feedback. The normal model servo interface does not offer any feedback about the torque, actual position temperature etc... One of the test stand reliability issues was that we were never 100% sure that the valve went where commanded, these actuators fix that problem. I've ordered some zero backlash couplers and when they come in I will mount the dynamixel opposite the plug valve and test the combination.
When we get to the point of flying to significant altitudes the brushed motors in these actuators and all standard model/robot servos are not acceptable. brushed motors have arcing problems at high altitude. So we have been testing a sensored brush less motor with a planetary gearbox and a ball valve. This may become the Lox valve for our system. I'm also looking at a small brush less motor as a replacement for the Tonegowa main motors. Below is a "teamnovak" brush less crawler motor attached to a bane bot gearbox and a 3 pc ball valve. This combination has an insane amount of torque and very precise control.
Controls/Helicopter.
I finally have the necessary sensors on the helicopter working 100% reliably in flight. The last item was to do a 3D hard iron calibration of the microstrain IMU so it would sense magnetic heading correctly. I've evaluate three sources of magnetic heading on the helicopter: (All three are still mounted)
1)The Crescent Vector two antenna GPS. With the 2nd antenna near the helicopter blades its very unreliable with the blades turning. The primary GPS info is fine, the 2nd RTK solution for heading is not very reliable, its almost useless.
2)The Ocean systems magnetic compass module out on the tail boom. Works fine when things are static, but seems very sensitive to vibration and acceleration.
3)The Microstrain IMU. After recalibrating the unit with all the electronics turned on and the blades spinning it works great. I just need to recalibrate after any configuration changes.
This will be the heading solution long term, its the best and seems to be the most reliable.
After getting the sensors working we started working on controlling things automatically. The first control to go under automatic control is heading. To test just heading I built rotary table I can run the helicopter on. Its is a lazy susan bearing between two pieces of plywood with the helicopter tie wrapped to some screwed down brackets (shown bellow)
This allowed me to quickly test my heading control code and get the system gains right in less than an hour. The weather in San Diego was such that I could not really fly this weekend, so I have yet to try the heading code in flight, but it works really well on the lazy susan. It yaws to true north when commanded at a fast but steady rate and holds that position when perturbed.
The data collection shows a tiny bit of overshoot when comming from more than 45 degrees away, but all in all I'm happy with it. the next control step will be to close the loop around commanded attitude using the RC system to command attitude and the IMU to measure attitude. That is my goal for this coming weekend.
If I stay with the four engine system the Swagelock plug valves are almost perfect for pressurization and fuel. (Won't work for Lox they freeze) One is shown below next to two dynamixel actuators.
These dynamixel actuators are robot servos with a an RS-485 interface will full feedback. The normal model servo interface does not offer any feedback about the torque, actual position temperature etc... One of the test stand reliability issues was that we were never 100% sure that the valve went where commanded, these actuators fix that problem. I've ordered some zero backlash couplers and when they come in I will mount the dynamixel opposite the plug valve and test the combination.
When we get to the point of flying to significant altitudes the brushed motors in these actuators and all standard model/robot servos are not acceptable. brushed motors have arcing problems at high altitude. So we have been testing a sensored brush less motor with a planetary gearbox and a ball valve. This may become the Lox valve for our system. I'm also looking at a small brush less motor as a replacement for the Tonegowa main motors. Below is a "teamnovak" brush less crawler motor attached to a bane bot gearbox and a 3 pc ball valve. This combination has an insane amount of torque and very precise control.
Controls/Helicopter.
I finally have the necessary sensors on the helicopter working 100% reliably in flight. The last item was to do a 3D hard iron calibration of the microstrain IMU so it would sense magnetic heading correctly. I've evaluate three sources of magnetic heading on the helicopter: (All three are still mounted)
1)The Crescent Vector two antenna GPS. With the 2nd antenna near the helicopter blades its very unreliable with the blades turning. The primary GPS info is fine, the 2nd RTK solution for heading is not very reliable, its almost useless.
2)The Ocean systems magnetic compass module out on the tail boom. Works fine when things are static, but seems very sensitive to vibration and acceleration.
3)The Microstrain IMU. After recalibrating the unit with all the electronics turned on and the blades spinning it works great. I just need to recalibrate after any configuration changes.
This will be the heading solution long term, its the best and seems to be the most reliable.
After getting the sensors working we started working on controlling things automatically. The first control to go under automatic control is heading. To test just heading I built rotary table I can run the helicopter on. Its is a lazy susan bearing between two pieces of plywood with the helicopter tie wrapped to some screwed down brackets (shown bellow)
This allowed me to quickly test my heading control code and get the system gains right in less than an hour. The weather in San Diego was such that I could not really fly this weekend, so I have yet to try the heading code in flight, but it works really well on the lazy susan. It yaws to true north when commanded at a fast but steady rate and holds that position when perturbed.
The data collection shows a tiny bit of overshoot when comming from more than 45 degrees away, but all in all I'm happy with it. the next control step will be to close the loop around commanded attitude using the RC system to command attitude and the IMU to measure attitude. That is my goal for this coming weekend.
Subscribe to:
Posts (Atom)